Originally Posted by
gedznz
I'm a hobbiest, not a machinest so had to make do with a lot of the process. This was my third attempt, first one was too rough, bent the second one rifling it when distracted ( yelling at the dog)
In short here's what I did
(1) shortened and spun the old HB between centers to get sections I could run in a steady rest that aligned with the bore. Thread to action
(2) drilled out the existing 303 HB. This was using chinesium HSS bits of varying lengths and sizes up to 11mm. Piloted bits would have been easier but the staged approached worked very well
(3) reamed the bore to final size. Had to use an extended adjustable reamer with a pilot. This was a horrible job as the reamer needed removing to clear chip about 100 times ( it seemed). A chucking reamer woudl have been easier but are too expensive for what was a test.
(4) pollished the bore with some 0000 steel wool
(5) pushed the button through with lots of oil using my 20 ton press and lots of vaious push rods.
(6) final lap with autosolv, crown, chamber and headspace. Cut extractor groove.